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Project YJ - Axle & Tcase Swap
Introduction
Preparation
Installation
Impressions
Costs
Thanks
Epilogue

 
 

 
 
Project YJ Articles
Introduction
Detailed History
Rubicon Express
Spring-Over
Bumper/Tire Rack
Rhino Liner
Scout Axle Swap
Detroit Lockers
vs. Lockrights
TeraLow Dana 300 4:1 Kit
Go 2 Twister Dana 300 Re-Indexer
Bestop Supertop
Transmission Overhaul
TJ Flares Install
Rocker Armour
Bestop TrailMax Aqua Sport Seats
Kilby Gas Tank Skid Plate
Teraflex Revolvers
Kilby High Volume Automatic Transmission Pan
Hi-Steer Conversion

 
 

Preparation

Front End

I started by completely disassembling the front end. The diff fluid was very muddy and contained water. I decided to have all new bearings and seals installed. But before I did that, I first had to address the issue of converting the housing into a spring-over axle configuration. Because the diff housing is so far to the side, the only reasonable way to do this was to grind a spring perch into the side of the housing. While I was at it, Rob convinced me to angle this new perch so that the pinion pointed towards the xfer case output. This provided extra ground clearance under the pinion yoke and allowed me to use a CV shaft. Grinding this perch into the housing was surprisingly easy.

Hub close-up When Rob & I dis-assembled the front end, it was obvious that I would have to replace all the bearings, seals, etc. This axle was heavily abused... but for $65, I wasn't disappointed The start of an SOA perch in the housing
This is the start of the perch mounting pad I ground into the top side of the front D44 (circled in red)
The finished front perch Once the mounting space was completed, I tack welded a half-inch thick plate to serve as the spring perch. I added four small gussets and then got John Edgar to weld it up for me at the same time he welded my yokes

The Scout axle has zero degrees of caster. Tilting the pinion upwards will result in negative caster. SOA conversions generally require five degrees or more of caster. It is for that reason that I had to adjust the axle yokes' caster. This was an excrutiatingly difficult process. I had to carefully grind away the welds which secured the yokes to the axle tubes and then pound on the yokes with a heavy hammer. After a lot of grinding and pounding, I finally got them moved to a decent angle. One thing to be aware of is that if you set them for too much caster, the steering arms may be tilted up so much that the drag link & tie rod will collide with the spring packs (applies only to SOA setups).

The crack which shows that the yoke can be turned When adjusting the yoke caster angles, I used an angle grinder with a thin wheel to grind away the weld securing the yoke to the axle tube. Here you can see the rust-coloured line which is the seam between the tube & yoke (indicated by a red arrow). If this line goes right around the tube, you can begin hammering the yoke to adjust its caster View of the two different caster angles In the foreground is the yoke which has been set to the new caster angle. In the background is the original caster. Big difference, eh?

Once the yokes were positioned just right, I had a professional welder weld the yokes in place using special rod which would work with the cast metal in the yokes. He also welded a spring perch plate onto the flat spot I ground into the housing. For the driver's side perch, I made one from square tubing and welded it on myself.

For shock mounts, I welded some simple studs onto the back of the housing so that they were perpendicular to the tube. I welded them directly to the tube because I wanted to eliminate all the annoying hardware that hung below the axles. I was planning on raising the upper shock mounts once I got my Jeep back on the road.

The housing was pretty filthy so I had it steam cleaned and re-painted. With that done, I handed all the pieces plus new bearings, seals, etc to Grant Klavatalks who re-assembled the front end and ensured that the ring & pinion gears were correctly setup. While he was doing that, I also had Grant drill & ream new holes in the steering arms so that I could mount my YJ tie rod six inches from the center of the ball joints. This would allow me to use the existing pitman arm without reducing my turning radius by very much. I also bought some 1976 Ford F150 4x4 front calipers rather than rebuilding the ones which were on the axle. I used Ford parts because they fit in the axles but used a smaller brake line fitting which was identical to the size already used on my YJ. I swapped the stock diff cover for one from a Ford reverse rotation D44. These covers are designed to be used on the front diffs so they are flattened in front for added tie rod clearance, they're approx 1/8" thick for rock protection, and the fill hole is higher up which is useful if your pinion is tilted high.

John Edgar welding the D44 housing With the front perch and yokes tacked in place, I hauled the front housing over to John Edgar's place where he welded everything up using rod which was amendable to joining cast & mild steel Top view of knuckle The new hole I had drilled for the YJ tie rod is circled in red. Turning radius is almost as good as before. You can also see the shock mount which I welded to the axle tube, raising it 3-4 inches higher than the factory YJ location

Rear End

In comparison, it was much easier to prepare the rear axle housing than the front. As with the front, I completely disassembled it and steam cleaned it. New bearings & seals were purchased, as were new brakes and drums.

The spring perches for the rear were purchased from Lou Feger's Racing (http://www.loufegersracing.com/). They were a clamp-on design which allowed me to mount the axle to my Jeep without welding the perches in place. This allowed me to adjust the pinion angle once the Jeep was resting on the wheels rather than trying to calculate/guesstimate what the pinion angle should be. I also had the option of adjusting the pinion angle after taking it for a few test drives. Then, once I found the perfect angle, I could weld the perches in place. The only fly in the ointment, so to speak, was that the adjustable perches were designed for Ford 9" axle tubes which are 3" OD, where as the Dana 44 tubes are 2.75" OD. To rectify this, I bought two short lengths of pipe with an OD of 3" and 1/8" wall thickness. Then I cut them in half lengthwise to fit them around the axle tubes where the perches were going to be mounted, and welded them in place. This brought the effective axle tube OD to 3". Lower shock mounts were similar to the front except that the studs ran parallel to the tube. They were mounted in line with the tube to maximize ground clearance.

Transfer Case

I purchased a yoke which would work with a CV shaft using 1310 u-joints. I also changed a couple of seals.


 
 
 

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